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Nitrogen+Syngas 367 Sept-Oct 2020

Improving nitric acid plant performance


NITRIC ACID PLANT MODERNISATION

Improving nitric acid plant performance

N. Temnaya and S. Suvorkin of NIIK report on the modernisation of monopressure (UKL-7) and dual pressure (AK-72) nitric acid plants in Russia and the CIS.

The main nitric acid manufacturing facilities in Russia and the CIS are based on large scale UKL-7 and AK-72 process units that are in need of upgrading.

Besides producing nitric acid, existing UKL-7 and AK-72 units generate thermal energy in the form of superheated steam which is fed into the plant’s network and mechanical energy which is generated in high-temperature gas turbines and is used for process air compression.

The main modernisation targets for existing UKL-7 and AK-72 units are to:

  • switch to a selective catalytic tail gas reduction system;
  • enhance unit capacity by reducing air consumption;
  • reduceeliminate natural gas consumption;
  • switch existing gas turbines to lower operating temperatures to increase their performance.

Research and Design Institute of Urea and Organic Synthesis Products (NIIK) is a leading design and technology company for chemical plants in Russia and the CIS. In co-operation with engineering and technical centre Khimazot-SPb LLC, NIIK is actively engaged in various projects for the modernisation projects of existing mono and dual pressure nitric acid units.

Currently NIIK is implementing two UKL-7 units modernisation designs which differ in the following ways:

  • gas turbine equipment available in the market;
  • process equipment design;
  • steam generation system used.

The first design is a new modernised UKL7-76M unit equipped with a GTT-3M gas turbine offering improved technical and economic performance (Fig. 1). The nominal capacity of the unit is 16.5 t/h nitric acid (HNO3 monohydrate).

Table 1: Comparison of the main features of UKL-7 units with different gas turbines
Table 2: The main parameters of the improved AK-72 unit

The second UKL-7 process design, currently in operation, uses a GTU-8 gas turbine unit, which is characterised by its smaller size and requires no intermediate air coolers or compensatory capacity of the drive. This scheme offers a quick return on capital investment and a compact and simpler plant arrangement (see Fig. 2).

The improvement of the existing mono-pressure UKL-7 unit benefits from:

  • 20% nitric acid capacity increase;
  • 30% reduction in natural gas consumption,
  • 15% increase of steam removal.

Going forward, a new single stage turbo-compressor unit TKT-88/7.6 will be introduced to the market as the latest NIIK REP Holding (Saint-Petersburg) development.

The TKT-88/7.6 turbo-compressor unit for new nitric acid plants is supplied as a single unit with a starting device, combustion chamber and aggregate equipment located in a noise-insulating casing on the support frame.

A distinctive feature of the TKT-88/7.6 gas turbine unit is the increased air capacity which has an output of 20 t/h min nitric acid (HNO3 monohydrate).

The new TKT-88/7.6 unit increases nitric acid output to 20 t/h min and reduces natural gas consumption (Table 1).

NIIK in cooperation with KhimAzot-SPb are also currently implementing the modernisation of a large scale AK-72 dual pressure unit. Fig. 3 shows the improved AK-72 nitric acid unit with selective catalytic tail gas reduction. In the proposed design, the gas turbine unit will be switched to low temperature conditions (550-590°C).

At the same time the capacity of the modernised AK-72 plant will be increased to 60 t/h nitric acid (HNO3 monohydrate) and the natural gas consumption will be reduced by 50%.

The main parameters of the improved AK-72 unit are specified in Table 2.

Figs 1, 2 & 3: Nitric acid plant modernisation

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